Aviation Accident Summaries

Aviation Accident Summary WPR12CA056

Waipahu, HI, USA

Aircraft #1

N817AB

ROBINSON HELICOPTER R22 BETA

Analysis

The certified flight instructor (CFI) and a student pilot, who held a foreign-issued fixed-wing certificate, were on a local training flight to practice autorotations. The CFI demonstrated the first autorotation. Prior to letting the student take the controls, she reviewed the recovery procedure again. The CFI remained on the controls while the student made the control applications. One autorotation was performed successfully. The student entered his second autorotation, and, at 1,000 feet above ground level, the CFI requested that the student perform a recovery. Rather than cracking the throttle as demonstrated, the student rolled on the throttle, and the CFI felt a yaw to the right. The CFI took control of the helicopter and countered the yaw with left pedal. The CFI noted that the engine rpm and rotor rpm were excessively high, so she decreased the throttle to lower the engine rpm. She began to raise the collective to lower the rotor rpm, but neither of the rpm needles decreased. The helicopter was maintaining a level attitude, but it was descending. During the landing, the low rotor rpm horn sounded, the helicopter touched down hard, and the tail boom separated. The CFI reported no preimpact mechanical malfunctions or failures with the helicopter that would have precluded normal operation.

Factual Information

The certified flight instructor (CFI) and a student pilot, who held a foreign-issued fixed-wing certificate, were on a local training flight. The purpose, in part, was to practice autorotations. The CFI demonstrated the first autorotation. The CFI entered the autorotation after saying "…entering autorotation in 3-2-1" and lowered the collective while simultaneously adding right pedal for trim. Once the collective was all the way down, she closed the throttle. The CFI began to recover at an altitude of approximately 1,000 feet by cracking open the throttle and letting the governor take over after 80 percent revolutions per minute (RPM). Prior to letting the student take the controls, she reviewed the recovery procedure again. The CFI remained on the controls while the student did the control applications. One autorotation was performed successfully. The student entered his second autorotation and at 1,000 feet above ground level, the CFI requested that the student perform a recovery. The student rolled on the throttle and the CFI felt a yaw to the right. The CFI countered with left pedal and stated "I have the controls" and the student relinquished all controls. The CFI noted that the engine and rotor RPMs were excessively high so she decreased the throttle to lower the engine RPMs. She began to raise the collective to lower the rotor RPM, but neither of the RPM needles decreased. The helicopter was maintaining a level attitude but got closer to the ground. As they neared the ground, she looked for a place to land. During the landing, the low rotor RPM horn sounded and the helicopter touched down on the ground. They exited the helicopter and saw that the tail boom had separated. The CFI reported no preimpact mechanical malfunctions or failures with the helicopter that would have precluded normal operation.

Probable Cause and Findings

The certified flight instructor's delayed remedial action and inadequate supervision during a practice autorotation. Contributing to the accident was the student pilot's excessive application of the throttle.

 

Source: NTSB Aviation Accident Database

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