Aviation Accident Summaries

Aviation Accident Summary WPR12FA339

Truckee, CA, USA

Aircraft #1

N8218P

PIPER PA-24-250

Analysis

Two witnesses who were onboard the airplane during an attempted takeoff before the accident flight stated that, during the takeoff, the airplane appeared to accelerate and lift off normally. However, as the airplane climbed about 20 feet above the runway, it wobbled to the left and right and drifted slightly to the left. The pilot subsequently aborted the takeoff. Upon returning to the terminal, the pilot had both passengers exit the airplane, and he then taxied back to the active runway. During the second attempted takeoff, several witnesses observed the airplane begin a normal takeoff roll, lift off about one-third of the way down the runway, and enter a nose-high attitude. The airplane was observed rotating back and forth along its longitudinal axis before entering a steep right turn. Subsequently, witnesses observed the airplane descend into an unoccupied hangar. All of the witnesses reported that the engine sounded normal and appeared to be producing power during the takeoff and accident sequence. Postaccident examination of the accident site and airplane wreckage revealed signatures consistent with a near-vertical impact with the hangar. Examination of the airplane, flight control systems, engine, and propeller revealed no evidence of any preimpact mechanical malfunctions or failures that would have precluded normal operation. At the time of the accident, the airplane was within weight and balance limitations. Review of the pilot's personal primary care medical records revealed treatment for shift-work sleep disturbance with zolpidem and treatment of hypertension with valsartan. On each visit, the primary physician recorded that the pilot reported no use of drugs or alcohol. Postaccident toxicology testing revealed positive results for losartan (also used to treat hypertension), zolpidem, and buprenorphine, which is a controlled substance used to treat severe pain. The pilot's primary care medical records did not mention acute or chronic pain or its treatment. Buprenorphine carries a warning from the Federal Drug Administration that it "may impair mental and/or physical ability required for the performance of potentially hazardous tasks (e.g., driving, operating heavy machinery)." Further, opiates cause, in part, sedation, alterations in cognitive and sensory efficiency, respiratory depression, nausea, vomiting, headache, and sleep and concentration disorders. With chronic use, tolerance can develop, which mitigates the drug's effects. Several issues made the interpretation of the toxicology report difficult. Opioids may undergo postmortem redistribution, which may result in postmortem levels not directly reflecting antemortem levels. In addition, depending on the pilot's pattern of use, it is possible that he had some degree of tolerance for the drug's effects. Further, his actual dosing interval may not have been the same as the dosing interval noted on the prescription bottle found in the airplane. Thus, it was not possible to determine the exact effects of the drug on the pilot at the time of the accident. In addition, the effects of the underlying chronic pain syndrome on the pilot's performance are unknown. However, it is likely that the pilot was using a significant amount of opiate medication at the time of the accident, and, therefore, that he was impaired to some degree as a result.

Factual Information

HISTORY OF FLIGHTOn August 2, 2012, about 0814 Pacific daylight time, a Piper PA-24-250, N8218P, sustained substantial damage when it impacted a hangar during takeoff initial climb from Truckee-Tahoe Airport (TRK), Truckee, California. The airplane was registered and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91. The commercial pilot, sole occupant of the airplane, was fatally injured. Visual meteorological conditions prevailed and no flight plan was filed for the local flight which was originating at the time of the accident. Representatives from Los Medicos Voladores reported to the National Transportation Safety Board (NTSB) investigator-in-charge (IIC) that the pilot was participating in a flight to Baja, Mexico for medical outreach along with two passengers. As part of their flight, they were transporting medical supplies. Two witnesses, who were previously onboard the airplane reported that the accident flight was the second attempted takeoff by the pilot. Prior to the first takeoff, the pilot and passengers loaded baggage into the aft baggage compartment and rear seat area. After a normal taxi out and pre-takeoff checks, the pilot initiated takeoff on runway 19. The passengers stated that the airplane appeared to have accelerated and lifted off normally, however, as the airplane ascended through about 20 feet above the runway, the airplane wobbled to the left and right, and drifted slightly to the left. The pilot told the passengers that something did not feel right and that the airplane was not climbing. Subsequently, the pilot aborted the takeoff and landed uneventfully on the remaining runway. During the taxi back to the terminal area, the pilot and his two passengers discussed various ideas why the airplane was not climbing, including potential weight and balance issues and center of gravity issues. The witnesses further reported that the pilot told them that he was going to try and takeoff alone in order to troubleshoot. Upon returning to the terminal area, the pilot had both passengers exit the airplane while the engine was still running, and the pilot taxied back to runway 19. The witnesses further stated that while observing the airplane takeoff a second time from runway 19, the takeoff roll seemed to be uneventful and the airplane lifted off about one-third down the runway and entered a nose high attitude. The witnesses said that the airplane seemed to wobble back and forth several times as it was ascending. One witness said that as the airplane was over the departure end of the runway, at an altitude of about 150 feet above the runway, it appeared to enter a right turn and bank. As the turn continued, the bank angle of the airplane increased beyond 90-degrees as it descended behind a hangar. Additional witnesses located within the vicinity of the accident site reported that the airplane lifted off normally and entered a nose high attitude as if it was going to "stall." The witnesses continued to watch the airplane continue its takeoff initial climb and noticed that it began to wobble back and forth prior to entering a right turn. Subsequently, witnesses observed the airplane descend into a hangar. All witnesses reported that during the takeoff and accident sequence, the engine sounded normal and appeared to be producing power. PERSONNEL INFORMATIONThe pilot, age 66, held a commercial pilot certificate with an airplane single-engine land, multi-engine land and an instrument rating. A second-class airman medical certificate was issued on February 13, 2012, with no limitations stated. The pilot reported on his most recent medical certificate application; that he had accumulated 2,000 total flight hours. Review of the pilot's logbooks revealed that as of the most recent entry dated July 7, 2012, he had accumulated a total of 1,736 hours of flight time of which 339.3 hours were in the accident make/model airplane, 2.7 hours within the previous 30 days, 7.3 hours within the previous 60 days, and 24.1 hours within the previous 90 days to the accident. AIRCRAFT INFORMATIONThe four-seat, low-wing, retractable-gear airplane, serial number (S/N) 24-3471, was manufactured in 1963. It was powered by a Lycoming O-540-A1D5 engine, serial number L-5889-40, rated at 250 horse power. The airplane was also equipped with a McCauley model B3D32C412 adjustable pitch propeller. Review of the Pilot Operating Handbook (POH) revealed that section IV, General Maintenance, part VI. Fuel Requirements, states in part "…Aviation Grade 91/96 Octane (minimum) fuel must be used in the Comanche. The use of lower grades of fuel can cause serious engine damage in a very short period of time." The POH further states in section II, part IV., Take-Off, Climb and Stalls:, that prior to takeoff, flaps should be in the "UP" position. Using the rate of climb vs. standard altitude performance chart for the PA24 with a 250 horse power engine, elevation of 5,900 feet msl, at gross weight, the calculated rate of climb was about 1,000 feet per minute. Review of the airframe and engine maintenance records revealed that the most recent annual inspection was completed on January 12, 2012, at a tachometer hour reading of 1,804.6 hours and engine time since major overhaul of 438.6 hours. The maximum gross weight for the airplane per Piper's operating limitations is 2,900 pounds. The maximum weight for the aft baggage area is 200 pounds. Various items removed from the accident site were weighed using a kitchen scale. The items located within the aft baggage area totaled 122 pounds and the items within the left rear seat totaled 18 pounds. Three bags, totaling 48 pounds were removed prior to investigational personnel arriving on scene by previous passengers on the airplane. The weight of the bags was not verified by the NTSB IIC. Using the last reported aircraft weight that was on file with the Federal Aviation Administration (FAA) from 1977 of 1,798 pounds (83.63 arm), 85 gallons of fuel, pilot weight of 190 pounds, weighed items within the baggage compartment and removed bags (170 pounds total), and rear seat baggage of 18 pounds, the airplane weighed about 2,709 pounds at the time of takeoff with a moment of 239345.4. This calculated to a CG of 88.33 inches, which was within the limits of the airplane. Refueling records obtained from the Truckee-Tahoe Airport revealed that the airplane was topped off with 33.5 gallons of 100 low lead (LL) fuel. Samples of the fuel were taken by airport personnel following the accident and were found to be free of contaminants. Fuel samples were subsequently shipped to a laboratory for further examination. Analysis of the fuel samples revealed that the octane level of the fuel was 97.1. No additional anomalies were noted. METEOROLOGICAL INFORMATIONA review of recorded data from the Truckee-Tahoe Airport automated weather observation station revealed at 0755 conditions were wind calm, visibility 10 statute miles, clear sky, temperature 6 degrees Celsius, dew point -4 degrees Celsius, and an altimeter setting of 30.33 inches of Mercury. Using the reported weather conditions and field elevation, the calculated density altitude was about 5,842 feet and a pressure altitude of about 5,523 feet. AIRPORT INFORMATIONThe four-seat, low-wing, retractable-gear airplane, serial number (S/N) 24-3471, was manufactured in 1963. It was powered by a Lycoming O-540-A1D5 engine, serial number L-5889-40, rated at 250 horse power. The airplane was also equipped with a McCauley model B3D32C412 adjustable pitch propeller. Review of the Pilot Operating Handbook (POH) revealed that section IV, General Maintenance, part VI. Fuel Requirements, states in part "…Aviation Grade 91/96 Octane (minimum) fuel must be used in the Comanche. The use of lower grades of fuel can cause serious engine damage in a very short period of time." The POH further states in section II, part IV., Take-Off, Climb and Stalls:, that prior to takeoff, flaps should be in the "UP" position. Using the rate of climb vs. standard altitude performance chart for the PA24 with a 250 horse power engine, elevation of 5,900 feet msl, at gross weight, the calculated rate of climb was about 1,000 feet per minute. Review of the airframe and engine maintenance records revealed that the most recent annual inspection was completed on January 12, 2012, at a tachometer hour reading of 1,804.6 hours and engine time since major overhaul of 438.6 hours. The maximum gross weight for the airplane per Piper's operating limitations is 2,900 pounds. The maximum weight for the aft baggage area is 200 pounds. Various items removed from the accident site were weighed using a kitchen scale. The items located within the aft baggage area totaled 122 pounds and the items within the left rear seat totaled 18 pounds. Three bags, totaling 48 pounds were removed prior to investigational personnel arriving on scene by previous passengers on the airplane. The weight of the bags was not verified by the NTSB IIC. Using the last reported aircraft weight that was on file with the Federal Aviation Administration (FAA) from 1977 of 1,798 pounds (83.63 arm), 85 gallons of fuel, pilot weight of 190 pounds, weighed items within the baggage compartment and removed bags (170 pounds total), and rear seat baggage of 18 pounds, the airplane weighed about 2,709 pounds at the time of takeoff with a moment of 239345.4. This calculated to a CG of 88.33 inches, which was within the limits of the airplane. Refueling records obtained from the Truckee-Tahoe Airport revealed that the airplane was topped off with 33.5 gallons of 100 low lead (LL) fuel. Samples of the fuel were taken by airport personnel following the accident and were found to be free of contaminants. Fuel samples were subsequently shipped to a laboratory for further examination. Analysis of the fuel samples revealed that the octane level of the fuel was 97.1. No additional anomalies were noted. WRECKAGE AND IMPACT INFORMATIONExamination of the accident site revealed the airplane impacted an enclosed airplane hangar on row E, about 924 feet northwest of runway 19, and about 4,166 feet from the approach end of the runway. Wreckage debris was located within about 350 feet of the main wreckage. The fuselage came to rest inverted on a heading of about 351 degrees magnetic along with the left wing and engine, within the hangar. A small portion of the fuel bladder and associated wing structure remained lodged within the roof structure on top of the hangar. The outer portion of the right wing was located outside of the hangar about 50 feet to the east. Portions of the right wing structure were found about 75-feet on the northwest side of the main wreckage. A propeller tip was located northwest of the accident hangar about 350 feet from the main wreckage. An impact crater was observed within the asphalt hangar floor which measured about 18 inches by 18 inches and was about 7 inches deep. Rotational ground scarring was observed extending from the crater. The hangar and ground impressions were found to be consistent with an almost vertical impact angle. The measured elevation of the accident site was about 5,901 feet. Examination of the wreckage revealed that the left wing was partially separated from the fuselage at the wing root area. The aileron remained attached to the wing via its respective mounts. The flap actuator jackscrew showed an extension of 15 threads which was consistent with a flap setting of about 10 degrees flaps down. Flight control continuity was established from the left aileron to the cockpit controls. However, the control cables were separated at an area near the control column. The separated control cables exhibited splayed signatures, consistent with overload. The left main landing gear was found in the extended and locked position. In addition, the landing actuator cable was found in the extended position. The right wing was separated in two main sections. One section separated outboard of the main landing gear. The inboard section including the main landing gear and fuel tank was found within the hangar adjacent to the fuselage. The outboard section of the right wing was found outside the hangar and exhibited a large impact impression on the leading edge about mid span of the flap. The impression extended aft to the flap structure. The flap actuator jackscrew exhibited an extension of 15 threads which is consistent with an approximate 10 degree flap down setting. The right aileron remained attached to its respective mounts. The aileron balance cable was separated near the center fuselage section and exhibited splayed signatures consistent with overload. The right aileron control cable was found secured to the bell crank and continuous to the wing root. The right main landing gear extension cable was in the extended position. The fuselage was in an inverted position. The right door structure was damaged and separated from the fuselage. The fuselage structure surrounding the cabin area was compressed. The left and right stabilators, rudder, and vertical stabilizer remained attached to the empennage. The stabilator trim tab remained attached via respective mounts. The stabilator trim actuator was measured and found to be in a position consistent with slightly nose up. Control continuity was established from the stabilator balance tube to the cockpit controls. The vertical stabilizer and rudder were in place and secure. Continuity was established from the rudder bell crank to the cockpit controls. The engine remained attached to the fuselage via the two upper engine attachments mounts. The two lower engine mounts were separated. All engine accessories remained attached to the engine via their respective mounts with the exception of the carburetor. The top spark plugs were removed and exhibited light gray color deposits within the electrode area. The top spark plugs exhibited normal wear signatures when compared to the Champion Check-A-Plug comparison chart. The internal areas of the cylinders were examined using a lighted borescope. All of the piston heads, cylinder combustion chambers, intake, and exhaust valves were unremarkable. The rocker arm covers were removed. The crankshaft propeller flange was bent and a portion was cut in order to rotate the crankshaft by hand. Rotational continuity was established throughout the engine and valve train. Thumb compression and suction was obtained on all cylinders. When the engine crankshaft was rotated by hand, equal movement of all of the intake and exhaust rocker arms was observed. The propeller hub assembly was fractured and all three propeller blades were separated. About 6 inches of the outboard tips of all three propeller blades. All three propeller blades exhibited blade twisting, chordwise scratching, and "S" bending. Postaccident examination of the airframe and engine revealed no evidence of preexisting mechanical malfunctions or failures that would have precluded normal operation. During the on-scene examination of the wreckage, prescription bottles of Zolipdem, Losartan, and Buprenorphine prescribed to the pilot were located within the wreckage. MEDICAL AND PATHOLOGICAL INFORMATIONThe Nevada County Coroner conducted an autopsy on the pilot on August 3, 3012. The medical examiner determined that the cause of death was "…Multiple blunt force injuries." The FAA's Civil Aeromedical Institute (CAMI) in Oklahoma City, Oklahoma, performed toxicology tests on the pilot. According to CAMI's report, carbon monoxide, cyanide, volatiles, and drugs were tested with negative results, and had positive results for 0.046 (ug/mL, ug/g) Buprenorphine detected in Liver, 0.011 (ug/mL, ug/g) Buprenorphine detected in Blood (Aortic), Losartan detected in Urine, Losartan detected in Liver, 0.026 (ug/mL, ug/g), Norbuprenorphine detected in Blood (Aortic), Norbuprenorphine detected in Liver, Zolpidem detected in Liver, and Zolpidem detected in Muscle. The FAA blue ribbon medical file, autopsy results, toxicology report, investigator's report, and personal medical records were reviewed by the Chief Medical Officer for the National Transportation Safety Board. According to the FAA blue ribbon medical file, this pilot was first medically certified in

Probable Cause and Findings

The pilot’s failure to maintain control of the airplane during initial climb. Contributing to the accident was the pilot’s impairment by prescription pain medication.

 

Source: NTSB Aviation Accident Database

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