Aviation Accident Summaries

Aviation Accident Summary CEN14LA349

Carthage, IL, USA

Aircraft #1

N9185G

AIR TRACTOR INC AT-502

Analysis

The commercial pilot was taking off for an agricultural application flight. The pilot stated that, during the takeoff, the engine did not lose power but that the airplane was unable to gain sufficient speed to climb. After realizing the airplane was not accelerating or climbing as expected, the pilot dumped the chemical load in an attempt to gain altitude. The airplane became airborne and cleared a pond at the end of the airstrip, but it then contacted a dirt bank and nosed over on the far side of the pond. A postaccident examination of the airplane revealed that the engine torque gauge, which a mechanic had installed in the airplane about 3.5 months before the accident, was for a lower powered engine. The installation of the wrong gauge resulted in the redline on the gauge being lower than it should have been and likely resulted in the pilot not having an accurate torque indication and using a lower power setting than needed for the takeoff.

Factual Information

On July 7, 2014, about 1615 central daylight time, an Air Tractor AT-502 airplane, N9185G, collided with a pond at the end of a private airstrip during takeoff in Carthage, Illinois. The pilot received minor injuries, and the airplane was substantially damaged. The airplane was registered to and operated by Air Assault LLC as a 14 Code of Federal Regulations Part 137 aerial application flight. Visual meteorological conditions prevailed for the flight, which not operated on a flight plan. The local flight was originating at the time of the accident. The pilot reported the airplane was loaded with 364 gallons of chemical and both fuel tanks were ¾ full. He stated the wind was calm and the outside temperature was 88 degrees Fahrenheit. The takeoff was being made with 10 to 15 degrees of flaps extended. The pilot taxied to the end of the runway and applied the brakes while advancing the engine power. He released the brakes and the torque increased to 1,550 foot-pounds within 3 seconds. He noted the propeller rpm was above 2,200 and the first third of the takeoff was normal. The tail lifted off the airstrip about 2/3 the way down the runway and not at the half-way point as the pilot expected, nor did the aircraft accelerate as the pilot expected. The pilot stated that at this point he was committed to the takeoff so he dumped the load and attempted to fly the airplane. The airplane became airborne and cleared a pond, but contacted a bank on the far side of the pond, and the airplane flipped inverted. The pilot stated the engine did not lose power during the takeoff and given the conditions of the day, it should have flown. A postaccident examination of the aircraft by a Federal Aviation Administration inspector revealed that the Pratt & Whitney PT6-27 engine had been replaced with a higher powered -34 engine. On March 21, 2014, a new torque gauge was installed in the aircraft. The torque gauge installed was for the lower powered -27 engine which resulted in the redline on the gauge being lower than it should have been.

Probable Cause and Findings

The airplane’s inability to climb out of ground effect, which resulted from the pilot using a lower power setting than needed for takeoff due to the mechanic’s installation of the wrong engine torque gauge.

 

Source: NTSB Aviation Accident Database

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