Aviation Accident Summaries

Aviation Accident Summary WPR15LA179

Glendale, AZ, USA

Aircraft #1

N44508

BURR EXPRESS 2000 RG

Analysis

The private pilot reported that, following a normal landing in the experimental amateur-built airplane, he applied beta thrust to decelerate the airplane and lightly applied the brakes. Suddenly, the left main landing gear collapsed, and the airplane swerved to the left. The airplane departed the runway surface and the left wing impacted a runway sign. Postaccident examination revealed that the left main landing gear actuator heim rod failed where the threads met the rod end; however, the rod was not made available for further examination, and the reason for the landing gear collapse could not be determined.

Factual Information

On May 29, 2015, about 1542 mountain standard time, a Burr Express 2000 RG, N44508, experienced a landing gear collapse during the landing roll at Glendale Municipal Airport (GEU) in Glendale, Arizona. The private pilot and one passenger were uninjured, and the airplane sustained substantial damage to the rudder and elevators. The airplane was registered to, and operated by, the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed and no flight plan was filed. The flight departed from GEU at about 1500. The pilot reported that he landed the airplane onto the runway normally. He applied beta thrust to decelerate the airplane and started to brake lightly. Suddenly, the left main landing gear collapsed and the airplane swerved to the left. The airplane departed the runway surface and the left wing impacted a runway sign. It traversed along the dirt when the right landing gear collapsed and the tail impacted the ground before sliding to a rest. During a postaccident examination by a Federal Aviation Administration Inspector it was revealed that the left main landing gear actuator heim rod failed where the threads meet the rod end. Given the location of the heim rod, the inspector was unable to view the fracture surface while the component was installed on the airplane. In addition, the inspector noted that the hydraulic line to the gear actuator was ripped. The National Transportation Safety Board Investigator-in-charge attempted to obtain the heim rod for further examination, however, the pilot had already repaired the airplane and the part was no longer available.

Probable Cause and Findings

A collapse of the left main landing gear for reasons that could not be determined based on the available information.

 

Source: NTSB Aviation Accident Database

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