Aviation Accident Summaries

Aviation Accident Summary WPR15LA234

Dixie, ID, USA

Aircraft #1

N52095

CESSNA 180J

Analysis

The commercial pilot was conducting a nonscheduled passenger flight. The pilot reported that, while he was turning the airplane to align it with the runway for takeoff, the right brake failed. The pilot subsequently intentionally ground looped the airplane to avoid elevated terrain near the runway, during which the right wing struck terrain. Postaccident examination of the right brake hydraulic line revealed that it was cracked where the line bends between the fuselage and main landing gear leg. It is likely that the crack caused a hydraulic fluid leak, which rendered the brake inoperative. Metallurgical examination of the fracture surface revealed fatigue striations and ratchet mark formations, consistent with a fatigue fracture.

Factual Information

On July 26, 2015, about 0830 mountain daylight time, a Cessna 180J, N52095, sustained substantial damage while taxiing for takeoff following a reported loss of the right brake control at the Wilson Bar USFS Airport (C48) Dixie, Idaho. The airplane was registered to a private individual and operated by SP Aircraft under the provisions of Title 14 Code of Federal Regulations Part 135. The commercial pilot and three passengers were not injured. Visual meteorological conditions prevailed and no flight plan was filed for the non-scheduled passenger flight. The flight was originating at the time with a planned destination of Boise Air Terminal/Gowen Field, Boise, Idaho. The pilot reported that the right brake failed while performing a 180 degree turn to align the airplane with the runway. As a result, the pilot stated that he intentionally ground looped the airplane, in order to avoid elevated terrain near the runway. Subsequently, the right wing struck terrain. Postaccident examination of the damaged airplane by a Federal Aviation Administration inspector revealed that substantial damage was sustained to the right wing and aileron. The right brake hydraulic line was observed to be cracked at a bend between the fuselage and the main landing gear leg. The airplane is equipped with a hydraulically actuated disc brake on each wheel. Each brake is connected by a hydraulic line to a master cylinder attached to each side of the pilot's rudder pedals. The appropriate section of the brake hydraulic line was removed and sent to the National Transportation Safety Board, Materials Laboratory Division, for a detailed examination. Electron microscope images revealed that the brake line fracture surface was consistent with a fatigue fracture. Fatigue striations and ratchet mark formations were observed.

Probable Cause and Findings

The failure of the right brake hydraulic line during taxi due to fatigue, which caused a loss of hydraulic fluid and rendered the brake inoperative.

 

Source: NTSB Aviation Accident Database

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