Aviation Accident Summaries

Aviation Accident Summary ERA16FA248

Hickory, KY, USA

Aircraft #1

N427TV

BELL HELICOPTER TEXTRON CANADA 407

Analysis

The pilot was performing a visual approach to a landing zone to board an additional crewmember. A witness reported that there were no abnormalities in the helicopter's sound or position, until it was approximately 75 to 100 feet above the ground. Suddenly, the main rotor tilted to the right. Immediately after, the entire helicopter banked to its right and fell to the ground on its right side, where it came to rest. The main rotor blades broke apart during the impact sequence. The engine continued to run after the accident, and was subsequently shut down by responding personnel. An examination of the wreckage revealed that the collective lever, located at the front and bottom of the swashplate support, was disconnected from the pivot sleeve. The collective lever was designed to move the pivot sleeve vertically on the swashplate support, via direct linkage from the cockpit collective control, to change the pitch on all the main rotor blades simultaneously. The collective lever pins and screws that attached the collective lever to the pivot sleeve were missing; they were later found loose, near the main rotor area. The safety wires intended to secure the screws to the pins were missing. Examination of the hardware at the NTSB Materials Laboratory revealed that the safety wires not present, and the screws backed out over time, resulting in the complete loss of collective control in flight. Maintenance on the helicopter was performed about 38 flight hours prior to the accident. The maintenance included a 24-month inspection that required examination of the flight control bolts and nuts. The collective lever pins were not specifically included in that inspection. Two mechanics and a maintenance foreman, all employees of the operator, performed the maintenance, and all reported during postaccident interviews that they did not recall removing the safety wire or examining the pins. However, the foreman added, "I could see why it [examination of the collective lever pins] could have been done. The 24-month flight control bolt inspection was being performed, why not pull them and look at them too. I've done it before." Two of the mechanics reported that they would occasionally be "pulled off" one aircraft to work on another, and there was no work interruption policy in place. Thus, given that the safety wires were missing, it is likely that they were removed and not replaced during the most recent maintenance and that maintenance personnel did not recall taking that action due to possible work interruptions. Subsequent to the accident, the operator implemented numerous safety initiatives to prevent recurrence, including two independent safety audits, a formal fatigue risk management program, a Safety Management System, a formal tool/material accountability program, new work interruption policies, creation of a formally-trained Safety Officer position, and a formal process for the communication of safety-critical information.

Factual Information

HISTORY OF FLIGHTOn July 11, 2016, at 1123 central daylight time, a Bell 407, N427TV, collided with terrain during the approach to landing at the Tennessee Valley Authority (TVA) Mayfield Customer Service Center, Hickory, Kentucky. The commercial pilot was fatally injured, and the helicopter was substantially damaged by impact forces. The helicopter was registered to and operated by the TVA under the provisions of 14 Code of Federal Regulations Part 91 as a business flight. Day visual meteorological conditions prevailed, and no flight plan was filed. The flight originated from Outlaw Field Airport (CKV), Clarksville, Tennessee at 1048. According to TVA personnel, the pilot flew the helicopter from Knoxville, Tennessee, to CKV, refueled, and then flew to the TVA Customer Service Center to pick up a maintenance lineman for the purpose of inspecting power lines and equipment. According to a TVA lineman who witnessed the accident, there was a light wind from the south/southeast, and the helicopter appeared to be making its final approach from the north. The witness stated that there were no abnormalities in the helicopter's sound or position, until the helicopter was about 75 to 100 ft above the ground. He then observed the main rotor abruptly tilt to the right. Immediately after, the helicopter banked right, fell to the ground, and came to rest on its right side. The witness stated that he never lost sight of the helicopter and described the impact as very hard with no sliding or bouncing. He saw the rotor blades break apart. The witness then ran into the building to get help. The helicopter's engine continued to run after the accident and was subsequently shut down by responding personnel. Initial examination of the wreckage revealed that the collective lever, which connected the cockpit collective controls to the main rotor, was disconnected from the pivot sleeve. The attaching hardware for the lever was subsequently found loose in the wreckage near the main rotor hub. PERSONNEL INFORMATIONThe pilot, who was seated in the right cockpit seat, held a Federal Aviation Administration (FAA) commercial pilot certificate with airplane single-engine land, rotorcraft-helicopter, instrument airplane, and instrument helicopter ratings. He held an FAA second-class medical certificate with a restriction to wear corrective lenses. The pilot reported 18,430 total hours of flying experience on his latest medical certificate application, which was dated March 31, 2016. TVA personnel reported that his flight experience in the Bell 407 was about 850 hours. He completed a flight review in a MD Helicopters MD530 helicopter on February 12, 2016, and a flight review in the Bell 407 on January 5, 2016. AIRCRAFT INFORMATIONThe helicopter was a Bell Helicopter model 407, serial number 54106, built in 2012 and purchased new by the TVA. It was a single-engine helicopter of conventional construction and equipped with a four-blade, soft-in-plane design, composite hub, main rotor system, a full monocoque aluminum-skinned tail boom, and a conventional two-blade tail rotor system. The helicopter was powered by a Rolls-Royce model 250-C47B turboshaft engine, serial number CAE-848434, with maximum takeoff and maximum continuous power ratings of 650 and 600 shaft horsepower, respectively. The helicopter was issued a normal category standard airworthiness certificate and was maintained under an approved aircraft inspection program. Between May 31, 2016, and June 20, 2016, the helicopter was at the TVA maintenance facility at Muscle Shoals, Alabama, and the following inspections were accomplished: annual/50hr/100 hr, 150hr, 300 hr, 300hr/12 month, 600hr/12 month, 1200 hr/2 year, 12-month and 24-month inspections. From June 20, 2016, until the time of the accident, the helicopter was operated about 38.4 hours. The collective lever was located at the front and bottom of the swashplate support. The collective lever and collective control link were designed to move the pivot sleeve vertically on the swashplate support to change the pitch on all the main rotor blades simultaneously. The collective lever was attached to the pivot sleeve with screws, washers, and pivot pins (see figure 1). Once attached, the and the specified torque was applied, locking wire would typically be affixed to the screw. Figure 1 - Swashplate support assembly, with collective pitch lever attaching hardware outlined in red. The maintenance tasks performed during the inspections between May 31, 2016, and June 20, 2016, did not require the removal of the collective lever or the disconnection or inspection of the collective lever pins or screws. Although an inspection of the condition of the flight control bolts and nuts was one of the maintenance tasks performed, an inspection of the collective lever pins, screws, and corresponding lockwire was not included in that inspection. The maintenance and inspections of the helicopter's flight controls, including the collective control, were performed by two TVA airframe and powerplant mechanics and one TVA foreman, who assisted in the work and supervised the operation. All three employees were interviewed by FAA inspectors following the accident. One of the mechanics re-installed an anti-drive lever assembly. He did not recall removing the lockwire on the collective lever pin screws or removing the pins. He stated that the other mechanic performed the 24-month inspection of the flight control bolts and nuts. He further stated that the collective lever pins were not part of that inspection. The other mechanic performed the 24-month inspection of the flight control bolts and nuts. When asked if he removed the collective lever pins, he responded, "No, I don't remember doing it. If anyone would have done it, it would have been me, but I don't remember doing it." The foreman inspected the work performed in the area of the flight controls. He reported that the removal of the collective lever pins "…was not part of the required maintenance performed." He was not aware that the pins were removed or that any lockwire was removed. He added further, "I could see why it could have been done. The 24-month flight control bolt inspection was being performed, why not pull them and look at them too. I've done it before." Both mechanics reported that they would occasionally be "pulled off" an aircraft to perform work on another project. One mechanic stated that there was a lack of documentation of what parts were removed, such as a continuation sheet. METEOROLOGICAL INFORMATIONMayfield - Graves County Airport (M25), Mayfield, Kentucky, was the closest official weather station, which was 8 miles from the accident location. The M25 weather at 1135 included wind from 120° at 5 knots, visibility 10 statute miles, scattered clouds at 1,000 and 2,200 ft, overcast ceiling at 10,000 ft, temperature 26°C, dew point 22°C, and altimeter setting 30.06 inches of Mercury. AIRPORT INFORMATIONThe helicopter was a Bell Helicopter model 407, serial number 54106, built in 2012 and purchased new by the TVA. It was a single-engine helicopter of conventional construction and equipped with a four-blade, soft-in-plane design, composite hub, main rotor system, a full monocoque aluminum-skinned tail boom, and a conventional two-blade tail rotor system. The helicopter was powered by a Rolls-Royce model 250-C47B turboshaft engine, serial number CAE-848434, with maximum takeoff and maximum continuous power ratings of 650 and 600 shaft horsepower, respectively. The helicopter was issued a normal category standard airworthiness certificate and was maintained under an approved aircraft inspection program. Between May 31, 2016, and June 20, 2016, the helicopter was at the TVA maintenance facility at Muscle Shoals, Alabama, and the following inspections were accomplished: annual/50hr/100 hr, 150hr, 300 hr, 300hr/12 month, 600hr/12 month, 1200 hr/2 year, 12-month and 24-month inspections. From June 20, 2016, until the time of the accident, the helicopter was operated about 38.4 hours. The collective lever was located at the front and bottom of the swashplate support. The collective lever and collective control link were designed to move the pivot sleeve vertically on the swashplate support to change the pitch on all the main rotor blades simultaneously. The collective lever was attached to the pivot sleeve with screws, washers, and pivot pins (see figure 1). Once attached, the and the specified torque was applied, locking wire would typically be affixed to the screw. Figure 1 - Swashplate support assembly, with collective pitch lever attaching hardware outlined in red. The maintenance tasks performed during the inspections between May 31, 2016, and June 20, 2016, did not require the removal of the collective lever or the disconnection or inspection of the collective lever pins or screws. Although an inspection of the condition of the flight control bolts and nuts was one of the maintenance tasks performed, an inspection of the collective lever pins, screws, and corresponding lockwire was not included in that inspection. The maintenance and inspections of the helicopter's flight controls, including the collective control, were performed by two TVA airframe and powerplant mechanics and one TVA foreman, who assisted in the work and supervised the operation. All three employees were interviewed by FAA inspectors following the accident. One of the mechanics re-installed an anti-drive lever assembly. He did not recall removing the lockwire on the collective lever pin screws or removing the pins. He stated that the other mechanic performed the 24-month inspection of the flight control bolts and nuts. He further stated that the collective lever pins were not part of that inspection. The other mechanic performed the 24-month inspection of the flight control bolts and nuts. When asked if he removed the collective lever pins, he responded, "No, I don't remember doing it. If anyone would have done it, it would have been me, but I don't remember doing it." The foreman inspected the work performed in the area of the flight controls. He reported that the removal of the collective lever pins "…was not part of the required maintenance performed." He was not aware that the pins were removed or that any lockwire was removed. He added further, "I could see why it could have been done. The 24-month flight control bolt inspection was being performed, why not pull them and look at them too. I've done it before." Both mechanics reported that they would occasionally be "pulled off" an aircraft to perform work on another project. One mechanic stated that there was a lack of documentation of what parts were removed, such as a continuation sheet. WRECKAGE AND IMPACT INFORMATIONGeneral The helicopter came to rest on its right side, about 220 ft west of the intended landing zone (LZ). The LZ was a level, open, gravel-covered storage area for power transmission equipment. All four main rotor blades separated from the main rotor hub during the impact sequence. The aft section of the tail boom severed from the fuselage, and the tail rotor assembly remained attached to the aft section of the tail boom. Fuel and Hydraulic Systems The helicopter's fuel system was not compromised and contained about 695 pounds of fuel. No fuel leaks were observed, and all fuel hoses and lines were secure. The airframe-mounted fuel filter was clean, and the fuel inside was clear with no particulates noted. Hydraulic fluid was observed in the hydraulic system reservoir. All lines and hoses were secure, and there were no leaks noted. Landing Gear The right skid of the landing gear was fractured fore and aft, above the saddle. The right step was separated due to fractured brackets. There was an impact mark on the aft portion of the right skid that matched the general size and shape of a ground scar at the point of initial ground impact. The front cross tube remained attached to the fuselage by one bracket, and the rear cross tube was not attached to the fuselage due to fractures at the support brackets. Fuselage The forward fuselage exhibited crushing damage on its right side along the bottom of the fuselage. The center post of the windscreen was fractured at the bottom. The battery cover on the nose was damaged near the hinged area near the bottom of the center post. The transmission deck exhibited minor damage to its right side. Main and Tail Rotor Systems Examination of the main rotor blades revealed that all four rotor blades were fractured. The yoke exhibited fracturing near all four inner elastomeric shear bearings with "strawing" signatures on the flexures. The blue pitch link was bent outward towards the top with all pitch link hardware present and all cotter keys installed. The red and orange pitch change links were undamaged with pitch link hardware present and all cotter keys installed. The green pitch change link was bent and fractured from impact forces and was found near the main wreckage. Each blade exhibited bending and delamination. All blades exhibited ground impact marks on the leading edges. Main rotor continuity was confirmed by rotating the drive shaft by hand. Movement was confirmed from the drive shaft through the transmission to the mast. The transmission was visually inspected and no pre-impact anomalies were observed. The chip detectors were removed and visually inspected with no ferrous particulate matter observed. No abnormal sounds were heard when the transmission was rotated by hand. The transmission was not disassembled. The tail boom was fractured near the aft bulkhead, just aft of the intercostal support and the fracture surfaces were consistent with a counter-clockwise main rotor strike to the ground. The vertical fin displayed scraping damage on its lower, outboard side, and the anti-collision light remained intact. The tailskid remained attached. Both the left and right finlets on the horizontal stabilizer were fractured and missing from the stabilizer from impact forces. Both tail rotor blades exhibited minor ground impact damage; however, no rotational scoring was observed on either blade. The tail rotor was easily rotated in both directions with no abnormal binding or noises. The pitch of the tail rotor blades was manipulated by hand with appropriate control movement noted forward to the aft end of the fractured control tube. The flapping stops exhibited compression signatures with corresponding impact marks on the yoke. The forward end of the forward short shaft remained attached to the output end of the freewheel unit. The aft end of the forward short shaft remained attached to the forward end of the oil cooler blower shaft. The oil cooler blower shaft was rotated by hand with slight binding due to shifting of the forward end of the aft short shaft. The forward end of the aft short shaft remained coupled with the aft end of the oil cooler blower shaft. The aft end of the aft short shaft remained connected to the hanger bearing. Rotational scoring was observed on the aft short shaft with signatures indicative of contact with the engine oil tank bracket. The forward end of the #4 tail rotor drive shaft segment was separated. The #3 and #2 tail rotor drive shaft segments were separated from the tail boom and were found adjacent to the main wreckage. The forward end of the #1 tail rotor drive shaft segment was connected to the hangar bearing with the aft end of the #1 tail rotor drive shaft segment connected to the input shaft of the tail rotor gear box at the Thomas coupling. Oil was evident in the tail rotor gear box. No chips were observed on the gear box chip detector. Flight Controls The left collective control was not installed. Collective control continuity was confirmed through the right collective and up through the servo actuators to the disconnected collective lever. The two collective lever pivot pins and screws that attached the collective lever to the pivot sleeve were not installed. The pivot pins and screws were found on the transmission deck and on the ground underneath the right side of the helicopter. The flat washers and lockwire were missing; the washers were later found during a subsequent examination of the

Probable Cause and Findings

Company maintenance personnel's inappropriate removal without replacement of the safety wires on the collective lever pin screws during a recent maintenance inspection, which resulted in the screws backing out and led to a loss of collective control in flight.

 

Source: NTSB Aviation Accident Database

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