Aviation Accident Summaries

Aviation Accident Summary WPR16LA149

Lancaster, CA, USA

Aircraft #1

N5103

SWARTZ GENE TITAN T 51 MUSTANG

Analysis

The private pilot reported that, while flying the experimental, amateur-built airplane in the airport traffic pattern, the engine experienced a total loss of power. He quickly attempted an engine restart, but was unsuccessful and decided to land on a nearby road. The airplane landed hard and the right main landing gear collapsed. The airplane subsequently veered to the right and impacted a sign. Postaccident examination of the engine revealed that a loose magnet in the flywheel struck the attachment bracket for the primary and secondary ignition, which disrupted the timing of the ignition system and rendered it inoperative; the engine subsequently experienced a total loss of power.

Factual Information

On July 23, 2016, about 1113 Pacific daylight time, an experimental amateur-built Swartz Gene, Titan T-51 Mustang, N5103, sustained substantial damage during a forced landing after a reported loss of engine power while on downwind at the General William J Fox Airfield (WJF) Lancaster, California. The private pilot and passenger were not injured. The airplane was registered to and operated by the pilot as a Title 14 Code of Federal Regulations Part 91 personal flight. Visual meteorological conditions prevailed, and no flight plan was filed. The local flight departed WJF about 1040. According to the pilot, the airplane was about 1,000 ft above ground level, initiating the base turn to final, when the engine lost power. He quickly attempted an engine restart but was unsuccessful and decided to land on a nearby road. He selected full flaps over the road and landed hard. Subsequently during the landing roll, the airplane's right main landing gear collapsed, causing the airplane to veer to the right and strike a highway traffic sign, which resulted in substantial damage to the right wing. Postaccident examination of the airplane's engine, under the supervision of a Federal Aviation Administration inspector, revealed that while accessing the engine, a loose portion of a bolt was observed at the bottom of the cowling. It was determined that the loose bolt portion came from the timing pickup bracket that secures the primary and secondary electronic ignition pickups to the engine. The magnetic flywheel, a part of the ignition system, consisted of four magnets. One magnet became loose and backed out and then struck the secondary timing pickup. Markings were consistent with the impact. The impact force on the secondary timing pickup caused one of the two bolts on the support bracket to separate and break off. Subsequently, the bracket moved about 2 inches, to the right and aft, which effected the primary and secondary ignition system's timing and rendered them inoperative. The broken bolt was replaced and the attachment bracket was secured back into it's support. The engine started and ran on the primary ignition system with no anomalies noted. However, on the secondary ignition system, the engine could not be started due to the damage sustained to the secondary system.

Probable Cause and Findings

A total loss of engine power due to the separation of a flywheel magnet, which impacted the attachment bracket for the primary and secondary ignition and disrupted the timing of the ignition system, rendering it inoperative.

 

Source: NTSB Aviation Accident Database

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