Aviation Accident Summaries

Aviation Accident Summary WPR17LA050

Kingman, AZ, USA

Aircraft #1

N605SJ

DIAMOND AIRCRAFT IND GMBH DA 40 NG

Analysis

The pilot reported that, during cruise flight, the airframe began to shake, and he received a failure annunciation indication from both engine control units, followed by indications of an increase in oil temperature and a loss of oil pressure. He decided to perform a forced landing into a field, during which both wings impacted vegetation and the airplane sustained substantial damage. Subsequent examination revealed that a large quantity of engine oil had been expelled out of the engine breather tube and onto the belly of the airplane. Disassembly of the engine revealed heavy pitting to the piston crown and combustion chamber surfaces of the No. 1 cylinder. The damage appeared to be the result of a fatigue crack in the piston, which allowed combustion gases to create a gas path, which eventually tunneled through the piston. The path ultimately reached the lowest piston ring, allowing pressurization of the engine crankcase, resulting in the observed expulsion of oil. The crack appeared to have been initiated by a nick in the piston crown, possibly caused by ingestion of a foreign wire-like object, which was harder than the aluminum material that comprised the piston and cylinder head. A determination of the foreign object type could not be made, but there are multiple possibilities regarding the source. The induction side of the turbocharger had experienced a failure about 234 flight hours prior, and the induction-to-intake plenum was replaced 192 hours prior to the accident. A fragment of material, such as safety wire, could have been inadvertently left inside the unfiltered side of the induction system during those maintenance events and been ingested into the engine. The design of the air induction system incorporated filters for both normal and alternate air operations, and, as such, foreign object ingestion during operation was unlikely. The engine’s oil analysis history did not indicate any significant deviations throughout its service history. Such damage would likely have resulted in oil contamination; therefore, the crack likely began to propagate during the 90-hour period between the last oil analysis and the accident flight. Multiple similar piston failures have occurred to other engines in the series, seemingly initiated by either foreign object ingestion and damage or thermal overload due to an out-of-tolerance fuel injector, or a combination of both. The manufacturer released a mandatory service bulletin to address the fuel injector defects and a service letter to address the potential for foreign object ingestion following maintenance events. Although not contributing to the accident, during the investigation, a series of cracks were observed in the cylinder head of both the accident engine and a series of other similar engines. In one event, a crack led to a loss of coolant after the cooling system became over-pressurized. In all cases, the cracks had occurred before the engines had reached their service life. The FAA-certified engine was originally designed and manufactured for automobile use, and subsequently modified by the manufacturer for aviation use. As such, the engine was not operating in the manner (continuous high-power operation) for which it was originally designed. The significance of this finding could not be determined.

Factual Information

HISTORY OF FLIGHTOn December 29, 2016, about 1230 mountain standard time, a Diamond Aircraft DA40 NG, N605SJ, was involved in an accident near Kingman, Arizona. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. The pilot reported that, during level cruise flight about 9,500 ft mean sea level (msl), he felt the airframe shake, and a few minutes later, he received an engine control unit (ECU) A and B failure annunciation. While performing the emergency checklist, he noticed that the engine oil temperature was rising. He reduced engine power and the oil temperature began to drop; however, a short time later, the oil pressure dropped to zero. Having descended to 2,500 ft above ground level, he decided to perform a forced landing into a field. During the landing roll, both wings impacted vegetation, resulting in substantial damage. Subsequent examination revealed that the belly of the airplane was covered in a black-colored oil from the engine cowling to the tail skid. AIRCRAFT INFORMATIONThe airplane was manufactured in 2015 and was used exclusively for flight training. It was equipped with a liquid-cooled, four-cylinder, turbocharged, AE300 (E4-series) diesel-fuel engine manufactured by Austro Engines. It utilized a chain-driven, double overhead cam system with four valves per cylinder and incorporated a full authority digital engine control (FADEC) system, which controlled both the engine parameters and propeller governor. The engine’s air induction system comprised an inlet air plenum mounted to the cowling and routed via a hose to an air filter housing. The housing contained both the standard air filter and an alternate air inlet, which was protected with a fine mesh foreign object damage (FOD) screen. A hose directly connected the outlet of the housing to the inlet of the turbocharger compressor housing. The outlet of the compressor then routed to the engine’s intake system via an intercooler. The engine was originally manufactured by Daimler AG., as the Mercedes-Benz OM640 automobile engine, and was modified for aviation use by Austro Engines. The design was type-certified by the Federal Aviation Administration (FAA) with a time between overhaul (TBO) interval of 1,800 hours. The airplane was inspected under a progressive inspection program; the most recent inspection was completed on December 13, 2016, 40 flight hours before the accident. At the time of the accident, the engine had accrued 1,342 total flight hours. Maintenance records indicated that on October 14, 2016, 192 flight hours before the accident, an inspection of the engine induction system resulted in the replacement of the induction-to-intake plenum tube after a tear was found on its inner surface. On September 19, 2016, 234 flight hours before the accident, the turbocharger assembly was replaced after it seized during flight, resulting in a total loss of power and loss of oil. The event did not result in an accident and was ultimately reviewed by representatives from Austro Engines. It was determined that the turbocharger housing was damaged at an undetermined time, eventually causing the separation of the compressor wheel bolt. The bolt then struck the compressor wheel, resulting in seizure of the turbocharger. The engine was repaired, and the airplane was returned to service. AIRPORT INFORMATIONThe airplane was manufactured in 2015 and was used exclusively for flight training. It was equipped with a liquid-cooled, four-cylinder, turbocharged, AE300 (E4-series) diesel-fuel engine manufactured by Austro Engines. It utilized a chain-driven, double overhead cam system with four valves per cylinder and incorporated a full authority digital engine control (FADEC) system, which controlled both the engine parameters and propeller governor. The engine’s air induction system comprised an inlet air plenum mounted to the cowling and routed via a hose to an air filter housing. The housing contained both the standard air filter and an alternate air inlet, which was protected with a fine mesh foreign object damage (FOD) screen. A hose directly connected the outlet of the housing to the inlet of the turbocharger compressor housing. The outlet of the compressor then routed to the engine’s intake system via an intercooler. The engine was originally manufactured by Daimler AG., as the Mercedes-Benz OM640 automobile engine, and was modified for aviation use by Austro Engines. The design was type-certified by the Federal Aviation Administration (FAA) with a time between overhaul (TBO) interval of 1,800 hours. The airplane was inspected under a progressive inspection program; the most recent inspection was completed on December 13, 2016, 40 flight hours before the accident. At the time of the accident, the engine had accrued 1,342 total flight hours. Maintenance records indicated that on October 14, 2016, 192 flight hours before the accident, an inspection of the engine induction system resulted in the replacement of the induction-to-intake plenum tube after a tear was found on its inner surface. On September 19, 2016, 234 flight hours before the accident, the turbocharger assembly was replaced after it seized during flight, resulting in a total loss of power and loss of oil. The event did not result in an accident and was ultimately reviewed by representatives from Austro Engines. It was determined that the turbocharger housing was damaged at an undetermined time, eventually causing the separation of the compressor wheel bolt. The bolt then struck the compressor wheel, resulting in seizure of the turbocharger. The engine was repaired, and the airplane was returned to service. TESTS AND RESEARCHInitial examination revealed that the engine had not seized. Residual quantities of oil remained in the sump and the oil filter was clear. The engine was removed from the airplane and shipped to the facilities of Austro Engines in Austria, where a complete examination was performed under the supervision of the Austrian Civil Aviation Safety Investigation Authority. A series of examination reports were prepared by Austro Engines and independent testing facilities. These reports were reviewed by a specialist from the NTSB Materials Laboratory, who concurred with the findings. External examination revealed that the outer surfaces of the crankcase at the exhaust port of cylinder No. 1 were coated in oil, and oil had also pooled in the fuel injector well just below the oil separator and breather tube assembly. The engine was dissembled, revealing damage to the No. 1 piston and its associated cylinder bore. The piston crown was covered in oil and carbon and exhibited pitting and peening damage, concentrated around its outer circumference (see figure 1). Similar pitting damage to the piston crown was observed around the circumference of the accompanying cylinder head combustion surface (see figure 2). Figure 1. No. 1 piston crown, with hole and crack. Figure 2. No. 1 cylinder head. A 5-mm-wide hole was present on the wall of the piston crown bowl, and a crack emanating from the hole, traversing aft along the piston pin axis (see figure 1). The crack continued down the side of the piston skirt, crossing the three piston ring grooves and the upper face of the piston pin bore. The left and right sides of the piston skirt exhibited vertical score marks, corresponding to similar abrasions on the adjacent areas of the cylinder bores. The intake and exhaust valves were intact and undamaged. Removal of the piston from cylinder No. 1 revealed that the 1st and 2nd combustion rings exhibited material transfer and abrasions on their sealing faces. The oil scraper ring exhibited similar damage along with carbon buildup. A section of the scraper ring, about 1/6th of the total circumference, had detached revealing the inner spring. About 1/3 of the spring had detached, and a series of spring fragments were located in the oil sump. Piston Examination Examination of the crack revealed two fatigue fracture areas with different fracture origins. One fracture origin was located at the surface of the piston crown close to the edge of the bowl and appeared to begin at a notch in the surface. The notch was similar in scale and definition as the pitting observed around the crown (see figure 3). From the notch, the crack propagated toward the back side of the piston, where it reached the ring grooves and the cooling bore. In this area, a void had developed, connecting the hole in the piston dome to the cooling bore and the two lower ring groves. The walls of the void were granular in appearance and appeared consistent with the formation of a “gas channel” by hot combustion gasses penetrating the crack and eroding the piston material (see figure 4). The second fatigue fracture area was located between the void and the back side of the piston, where it propagated to the piston pin bore (see figures 3 and 5). The fracture origin had been obliterated by the progression of the gas channel. No foreign particles were located in the combustion chamber, and a detailed review of the imprints in the piston crown and cylinder head revealed multiple notches with similar sharp edge surface features. Two pitted imprints, along with exemplar undamaged aluminum piston surface material, were examined utilizing scanning electron microscopy with energy dispersive x-ray analysis. The exemplar areas were primarily composed of aluminum. No definitive material type was identified within the imprints; however, carbon, silicon, sodium, and iron were present in the pits at higher concentrations than the surroundings. Figure 3. First fatigue crack, with notch. Propagation direction indicated by arrows. Figure 4. Piston No. 1 cross section. Figure 5. Second fatigue crack with propagation direction indicated by arrows. Small circle indicates presumed initiation point. Oval indicates end of first crack at boundary with gas path. Fuel Injector Examination The fuel injectors were examined and tested at an independent facility. All appeared undamaged and exhibited light carbon buildup at their tips which did not impeded fuel flow. All injectors displayed similar and nominal fuel delivery, and disassembly did not reveal any mechanical anomalies or contamination. Oil Analysis The engine had been subject to regular oil analysis at about 100-hour intervals since new, with the last analysis occurring 89.6 engine hours before the accident. Review of the historical data indicated no clear deviation in the composition of materials in the oil, with the particle quantification index remaining at the same level throughout the life of the engine. Oil analyzed after the accident indicated increased levels of aluminum, silicon, and iron. Fuel Analysis A series of fuel tests was performed on the batch of fuel used to service the airplane. The sample passed all tests. Similar Loss of Engine Power Events with E4-series Engines Greece: A Diamond DA40 NG, registration SX-IFR, experienced expulsion of engine oil and a partial loss of engine power during flight in Greece on February 3, 2017. The pilot was able to land the airplane without incident. The engine (serial number E4A-00189) was removed and inspected at the facilities of Austro Engines. Disassembly revealed a similar hole on the rear wall of the No. 4 piston crown bowl, as well as a similar crack along the piston pin axis, and gas path through to the cooling bore and piston rings. The left and right sides of the piston skirt exhibited vertical score marks, corresponding to similar abrasions on the adjacent areas of the cylinder bores. Although the piston crown appeared to indicate damage due to prior foreign object ingestion, no crack initiating feature could be found. Subsequent examination of the fuel injector for that system indicated that its fuel flow was slightly higher than the tolerance allowed. Austro Engines determined that the cause of the crack was likely a combination of a mechanically weakened piston due to foreign particle damage and increased thermal load due to an out-of-tolerance fuel injector. At the time of the event, the engine had accrued 2,204 hours of operation, about 30% beyond its recommended TBO. France: A Diamond DA40 NG, registration F-HOUI, experienced a severe engine vibration during a training flight in France on February 10, 2018. The pilot performed an uneventful precautionary landing at the departure airport. Disassembly of the engine (serial number E4A-00119) by Austro Engines revealed a similar hole on the rear wall of the No. 2 piston crown bowl, as well as a similar crack along the piston pin axis and gas path through to the cooling bore and piston rings. Again, the piston crown exhibited multiple indications of pitting consistent with foreign object damage, with a notch present at the initiation point of the piston crack. At the time of the event, the engine had accrued about 1,257 hours of operation. Australia: A twin-engine Diamond DA-42 NG experienced a loss of oil pressure and oil quantity and a subsequent partial loss of engine power to the left engine during a training flight. A similar crack, hole, and gas path were observed in piston No. 4; however, there was no evidence of foreign object ingestion. Examination of the engine (serial number E4B-00040) by Austro Engines revealed that fuel injector No. 4 had likely sustained internal wear to its pilot valve, which resulted in excessive fuel flow. Austro Engines determined that the increased flow caused an increase in thermal load, which resulted in the piston cracking. At the time of the event, the engine had accrued about 1,441 hours of operation. On January 8, 2019, Austro Engines released Mandatory Service Bulletin MSB-E4-025/3, which required replacement of fuel injectors upon reaching a specific service life. On February 25, 2019, The European Union Safety Agency (EASA) mandated compliance with this service bulletin through airworthiness directive 2019-0041. United States: Review of the FAA’s service difficulty report database revealed what appeared to be a similar event that resulted in a hole in the piston of an E4 engine (serial number E4B-00169) installed in a DA42 airplane. The report indicated that the event was observed during a maintenance ground run on March 25, 2016, at a total engine time of 1,293 hours. The operator could not be reached for comment. Service Information Letter In October 2017, Austro Engines released service information letter SI-E4-010, subject, “Caution of foreign object damage during maintenance.” The letter warned that, on multiple occasions, foreign object damage had led to engine failure, and gave advice on covering engine openings and avoiding foreign object entry during maintenance. Cylinder Head Cracks During the investigation, cracks were observed within the combustion chambers bridging the intake and exhaust valves of cylinders Nos. 2 and 3 (see figure 6). Review of the other Austro Engines-investigated events revealed similar cracks in all three engines. Representatives from Austro Engines stated that the cracks in the cylinder head, “are not expected to restrict the functionality in any manner.” The Australian Transport Safety Bureau (ATSB) investigated an accident involving a DA40 NG airplane equipped with an E4 series engine on September 8, 2017 (ATSB report# AO-2017-090). Although not contributing to the accident, similar cracks were observed in the cylinder heads. While that investigation was in progress, another DA40 NG in the operator’s fleet experienced an engine coolant system over-pressurization and the coolant leaked (the design of the engine is such that the cylinder head contains passages adjacent to the combustion chambers through which coolant is passed). Inspection of that aircraft found cracking in six of the eight-cylinder valve pairs on the cylinder head. Inspections on the remaining aircraft in the operator’s fleet of five DA40 NG aircraft revealed similar cracks in all cylinder heads, none of which had reached the 1,800-hour TBO. Figure 6. Cracks in the No. 3 cylinder head between the inlet and exhaust valves

Probable Cause and Findings

The loss of engine oil pressure during cruise flight, which resulted in partial loss of engine power and necessitated a forced landing. The loss of oil pressure was the result of a failed engine piston, likely initiated by foreign object damage, which resulted in the pressurization of the crankcase and expulsion of the engine oil.

 

Source: NTSB Aviation Accident Database

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