Aviation Accident Summaries

Aviation Accident Summary ERA17LA347

Marathon, FL, USA

Aircraft #1

N3187V

BEECH 35

Analysis

The private pilot fueled the airplane to capacity before departing on a local photography flight. About 1 hour after departing, the pilot was climbing the airplane to cruise altitude for the return to the departure airport. About 800 to 1,000 ft above mean sea level, the airplane experienced a sudden, total loss of engine power over open water and beyond gliding distance to shore. The pilot prepared to ditch and attempted five engine restarts without success. The propeller continued to windmill as the airplane landed upright, but subsequently sank in about 12 ft of saltwater. The airplane was recovered 12 days later and a fuel sheen was observed in the area. The wreckage was examined following recovery and the engine crankshaft could not be rotated due to saltwater corrosion. Examination of the engine-driven fuel pump revealed that the drive shaft remained intact and could be actuated by hand with no anomalies noted. The engine and its ignition and induction systems could not be thoroughly examined or tested due to extensive saltwater corrosion; therefore, the reason for the loss of engine power could not be determined.

Factual Information

On September 16, 2017, about 0855 eastern daylight time, a Beech 35, N3187V, was substantially damaged while ditching in the Gulf of Mexico, following a total loss of engine power about 10 miles west of Marathon, Florida. The private pilot and passenger were not injured. The personal flight was operated by the private pilot and conducted under the provisions of Title 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed and no flight plan was filed for the flight that originated from Fort Lauderdale Executive Airport (FXE), Fort Lauderdale, Florida, about 0745.The pilot reported that he and a business partner planned to survey damage to his business partner's home on No Name Key, Florida. They flew to the home, circled it at a low altitude, took photographs, and began a climb back to cruise altitude for the return to FXE. About 800 to 1,000 ft above mean sea level, the airplane experienced a total loss of engine power. The pilot prepared to ditch as the airplane would not glide far enough to reach land. He also attempted two engine restarts with no success, and reported the emergency to air traffic control. The pilot attempted two more engine restarts using the wobble fuel pump and electric fuel pump. He then attempted another restart using the electric fuel pump with no success. The pilot added that the propeller continued to windmill during the restart attempts. The pilot landed on the water with the landing gear and flaps retracted. The airplane came to rest upright and both occupants were rescued by law enforcement personnel. According to the president of a recovery company, the airplane was recovered 12 days later, on September 28, 2017. The airplane appeared to be intact and was resting on a sandy bottom. When the airplane was floated to the surface of the water, a fuel sheen was observed on the water surface. Following recovery, no fuel or water was noted in the left wing fuel tank and approximately 1 gallon of a fuel and water mixture was recovered from the right wing fuel tank. The president of the recovery company added that he was unable to rotate the propeller, possibly due to corrosion. The pilot further stated that he used REC-90, a 90 octane, ethanol free gasoline in the airplane and stored the gasoline in his hangar. After every flight, he completely fueled the airplane from the gasoline storage to prevent condensation from accumulating in the fuel tanks. Prior to the accident flight, he last flew the airplane on September 11, 2017, for .6 hours and added 6 gallons of gasoline after he landed. He also inspected the fuel tanks during the preflight inspection for the accident flight, and both fuel tanks were full. He recalled being burned from fuel in the water and noted that a recovery diver made the same comment. The pilot subsequently provided a receipt indicating that he most recently purchased 30 gallons of REC-90 on September 5, 2017. Initial examination of the wreckage by a Federal Aviation Administration inspector revealed that the fuselage was buckled during the ditching. The inspector further examined the wreckage at a recovery facility and specifically examined the engine driven fuel pump as the pilot thought that the pump might have failed. The engine driven fuel pump drive shaft remained intact. The inspector was able to actuate the pump by hand and did not note any anomalies with the pump. Due to extensive corrosion damage, the inspector was unable to rotate the engine crankshaft. The four-seat, low-wing, retractable tricycle-gear airplane, serial number D-623, was manufactured in 1947. It was powered by a Continental E185, 185-horsepower engine, equipped with a constant-speed, two-blade Hartzell propeller. The airplane's most recent annual inspection was completed on April 27, 2017. At that time, the airframe had accumulated 3,768.4 hours of operation and the engine had accumulated 72 hours since major overhaul. The airplane had flown about 35 hours, from the time of the most recent annual inspection, until the accident.

Probable Cause and Findings

A total loss of engine power for reasons that could not be determined because saltwater corrosion precluded a complete examination.

 

Source: NTSB Aviation Accident Database

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