Aviation Accident Summaries

Aviation Accident Summary CEN18LA206

Copemish, MI, USA

Aircraft #1

N369SL

HUGHES AERO CORP PREDATOR "C"

Analysis

The sport pilot and a passenger departed in a powered-parachute from the pilot's airstrip with calm winds. No anomalies were detected during the preflight inspection. After departure, the powered-parachute would not climb above 8 ft above ground level and was approaching 20-ft-tall trees. The pilot attempted to land between a wire fence and the tree line, and the powered-parachute subsequently impacted the ground and a tree base. The pilot reported that there were no mechanical malfunctions during the flight and stated that the air was "heavier" than expected. The field elevation at a nearby airport was 634 ft mean sea level (msl), and the calculated density altitude was about 2,821 ft msl. A review of a recent aerial photograph of the pilot's property showed a mowed 600-ft-long runway with a northwest-southeast orientation. At the time of the accident, no runway could be seen on the property because the grass was between 6 and 12 inches tall and appeared unused except for the accident flight. The unmowed runway and high-density altitude conditions likely affected the powered-parachute's takeoff performance, which resulted in the aircraft being unable to clear the trees near the runway.

Factual Information

On May 29, 2018, about 1958 eastern daylight time, a Hughes Aero Corporation Predator "C" powered parachute, N369SL, impacted trees and terrain during a forced landing following a takeoff from a private airstrip near Copemish, Michigan. The pilot and passenger sustained serious injuries. The powered parachute received minor damage during the impact sequence. The powered parachute was registered to and operated by a private individual as a Title 14 Code of Federal Regulations Part 91 personal flight. Day visual meteorological conditions prevailed in the area about the time of the accident, and the flight was not operated on a flight plan. The local flight was originating airstrip at the time of the accident.According to the pilot, the wind was calm all day of the accident flight. The purpose of the flight was to demonstrate the powered parachute to a potential buyer. He called a local airport for recorded weather. The pilot arranged the powered parachute for a northwest departure from his property. He warmed up the engines and checked gauges. The pilot checked all lines and the condition of the parachute. The pilot explained the flight to the passenger, buckled him in, and put on his helmet. The pilot got in the pilot seat and put a helmet on. The pilot started the takeoff run. The pilot added that he has a landmark tree where he would abort a takeoff if he was not airborne by that point. However, on the accident flight he was about 8 ft above ground level at that point. The pilot realized that something was not right and that the powered parachute would not climb. The powered parachute was approaching 20 ft trees. The pilot attempted to land between a wire fence and the treeline. The powered parachute impacted the ground and a base of a tree. The pilot reported that there were no mechanical malfunctions during the flight and stated that the air was "heavier" than expected or the passenger was pulling down on the tail lines. Pulling on the tail lines can cause the parachute to "stall or land." At 1957, the recorded weather, about 17 nautical miles and 295 degrees from the accident site, at the Frankfort Dow Memorial Field, near Frankfort, Michigan, was wind calm; visibility 10 statute miles; sky condition clear; temperature 30° C; dew point 18° C; altimeter 29.87 inches of mercury. The field elevation at the airport was 634 ft above mean sea level and the calculated density altitude there was about 2,821 ft above mean sea level. A Federal Aviation Administration Inspector examined the wreckage and did not detect any preimpact anomalies that would have precluded operation of the powered parachute. The Inspector reviewed a 2015 aerial photograph of the pilot's property that showed a mowed 600-foot runway with a NW-SE orientation. At the time of the accident no runway could be detected on the property as the grass was 6 to 12 inches tall and appeared unused but for the accident flight.

Probable Cause and Findings

The pilot's improper decision to take off with a passenger in high-density altitude conditions from a runway with tall grass present, which resulted in the powered-parachute's poor takeoff performance and its inability to clear a tree line and led to a subsequent forced landing.

 

Source: NTSB Aviation Accident Database

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