Aviation Accident Summaries

Aviation Accident Summary GAA18CA532

London, KY, USA

Aircraft #1

N230DE

Cessna 206

Analysis

The pilot reported that, during a touch-and-go landing, just after the airplane touched down, he reduced the flaps to 10° and applied full throttle for takeoff. While increasing airspeed, the airplane drifted left. He added right rudder, but the airplane continued to drift left, so he reduced engine power. The airplane then exited the left side of the runway, and the pilot briefly applied full throttle to cross a drainage ditch, and the airplane became airborne. Subsequently, when the airplane touched back down, the front landing gear separated from the airframe, and the airplane came to rest nose down. The airplane sustained substantial damage to the right wing and fuselage. The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation. The automated weather observation system at the airport reported that, about the time of the accident, the wind was from 100° at 3 knots. The pilot was performing a touch-and-go landing on runway 24.

Factual Information

The pilot reported that during a touch and go landing, just after the airplane touched down, he reduced the flaps to 10° and applied full throttle for takeoff. While increasing airspeed, the airplane drifted to the left. He added right rudder, but the airplane continued to drift left so he reduced engine power. The airplane then exited the left side of the runway and he briefly applied full throttle to cross a drainage ditch and the airplane became airborne. Subsequently, when the airplane touched back down, the front landing gear separated from the airframe, and the airplane came to rest nosed down. The airplane sustained substantial damage to the right wing and fuselage. The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation. The automated weather observation system at the accident airport reported that, about the time of the accident, the wind was from 100° at 3 knots. The pilot was performing a touch and go on runway 24.

Probable Cause and Findings

The pilot’s failure to maintain directional control during takeoff with a tailwind.

 

Source: NTSB Aviation Accident Database

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