Aviation Accident Summaries

Aviation Accident Summary ERA22LA109

Lexington, SC, USA

Aircraft #1

N879CD

CIRRUS DESIGN CORP SR22

Analysis

The pilot reported that during cruise flight the oil annunciator light illuminated, the oil pressure decreased to zero, and the engine tachometer neared its maximum limit. Soon thereafter, the engine lost power. During the forced landing, the pilot activated the whole airplane parachute system at an altitude of about 2,000 ft above ground level. The airplane descended via the parachute and landed upright in a lake. The pilot and passenger were able to swim to shore and were not injured. The airplane’s fuselage and left elevator were substantially damaged during the landing. Postaccident examination of the engine revealed that all of the crankshaft connecting rod journals showed evidence of lubrication distress. Additionally, the No. 3 main journal bearing shifted, resulting in the blockage of the oil ports and elongation of the crankcase lock slot. The No. 6 connecting rod bearing was fused to the crankshaft journal. The No. 1 cylinder rod bearings were fused together on the crankshaft, and the bearing surface was smeared and torn. The bearing metal melted and re-solidified along the edges. It is likely that the shift of the No. 3 main journal bearing blocked the oil port and restricted oil to the engine and propeller, resulting in destruction of the bearing of the No. 6 cylinder. This likely resulted in the fracture of the connecting rod, breach of the crankcase, and the catastrophic failure of the engine. The engine overspeed reported by the pilot is consistent with a loss of oil pressure to the propeller governor, which would have lowered the blade pitch and increased engine rpm. Review of maintenance logbook records revealed the No. 2 cylinder was replaced about 500 hours before the accident flight, at which time the engine had accumulated about 2,420 hrs. It is possible that the crankcase thru bolts were incorrectly torqued after the No. 2 cylinder change about 500 hours before the accident flight, which could have resulted in a shift of the No. 3 main journal bearing.

Factual Information

On January 13, 2022, about 1326 eastern standard time, a Cirrus SR-22, N879CD, was substantially damaged when it was involved in an accident near Lexington, South Carolina. The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. According to the pilot, a preflight inspection of the airplane was conducted with no anomalies noted. He stated, “I checked the oil quantity and added one quart of oil.” The pilot conducted a run-up and departed for Charleston Air Force Base/International Airport (CHS), Charleston, South Carolina, on a visual flight rules (VFR) flight plan about 1300. About 20 minutes into the flight, at 5,500 ft, the pilot reported seeing a red oil annunciator light illuminate, which was followed by the oil pressure gauge falling to zero pressure. The pilot stated that the engine tachometer was near red line and that the engine sounded like it was over speeding, so he reduced the throttle to slow the engine. Soon thereafter, the engine stopped producing power and smoke emanated from the engine compartment. He radioed air traffic control and reported an emergency, then started looking for a place to land. He was over the middle of a large lake (Lake Murray), so he held off deploying the Cirrus Airframe Parachute System (CAPS) until he was closer to the shoreline. At 2,000 ft he deployed the CAPS and the airplane slowly descended to the water. The airplane remained afloat for a few minutes and continued to drift toward the shoreline with the parachute still inflated; however, the airplane eventually started to float further from the shore. At that point, the pilot and passenger exited the airplane and swam to the shoreline. Examination of the airplane by a Federal Aviation Administration inspector after its recovery from the lake revealed substantial damage to the fuselage and left elevator. Additionally, the engine exhibited a hole on the top of the case near the No. 6 cylinder. Postaccident examination of the engine revealed that all crankshaft connecting rod journals showed evidence of lubrication distress. Additionally, the No. 3 main journal bearing had shifted, resulting in the blockage of the oil ports and elongation of the crankcase lock slot. The No. 6 connecting rod bearing was fused to the crankshaft journal. The No. 1 cylinder rod bearings were fused together on the crankshaft, and the bearing surface was smeared and torn. The bearing metal had melted and re-solidified along the edges. Review of maintenance logbook records revealed that on December 4, 2015, the No. 2 cylinder was removed, repaired, and reinstalled at tachometer time 1,906.9 hours. The accident occurred at tachometer time 2,420 hrs. The engine had a manufacturer specified time between overhaul of 2,000 hours in service; however, there was no record of the engine having been overhauled.

Probable Cause and Findings

A loss of engine power due to a shift of the No. 3 main journal bearing, which resulted in blocked oil ports that restricted oil to the engine’s internal components and a subsequent catastrophic engine failure.

 

Source: NTSB Aviation Accident Database

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